Yuma Energy, Inc. provided an operational and corporate update for the second quarter ended June 30, 2019. During the second quarter, the Company has taken significant steps to arrest the recent declines of daily production. Specifically, the Company successfully installed a new jet pump on the Nettles 39-1 well, resulting in approximately 40 barrels a day of gross oil (bbl/d) or 15 bbl/d net production, up from 10 bbl/d gross prior to the workover. The Company also repaired the gravel pack on the State Lease 18194 well which has produced approximately 140 bbl/d gross, or 60 bbl/d net, for the most recent two weeks. Prior to the workover, the well was producing 90 bbl/d gross. The Company continue to diligently review operations and evaluate opportunities to improve production where those activities result in short payback periods.